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Drive Error List - Yaskawa

Display Name Cause Investigative Actions Corrective Actions
A.020 Parameter Checksum Error 1
(The parameter data in the SERVOPACK is incorrect.)
The power supply voltage suddenly dropped.  Measure the power supply voltage. Set the power supply voltage within the specified range, and set Fn005 to initialize the parameter.
The power supply went OFF while changing a parameter setting. Check the circumstances when the power supply went OFF. Set Fn005 to initialize the parameter and then set the parameter again.
The number of times that parameters were written exceeded the limit. Check to see if the parameters were frequently changed through the host controller. The SERVOPACK may be faulty. Repair or replace the SERVOPACK. Reconsider the method of writing parameters.
Malfunction caused by noise from the AC power supply or grounding line, static electricity noise, etc. Turn the power supply ON and OFF several times. If the alarm still occurs, there may be noise interference. Take countermeasures against noise.
Gas, water drops, or cutting oil entered the SERVOPACK and caused failure of the internal components. Check the installation conditions. The SERVOPACK may be faulty. Replace the SERVOPACK.
A SERVOPACK fault occurred. Turn the power supply ON and OFF several times. If the alarm still occurs, the SERVOPACK may be faulty. The SERVOPACK may be faulty. Replace the SERVOPACK.
A.021 Parameter Format Error 1
(The parameter data in the SERVOPACK is incorrect.)
The software version of SERVOPACK that caused the alarm is older than that of the written parameter. Check Fn012 to see if the set software version agrees with that of the SERVOPACK. If not, an alarm may occur. Write the parameter of another SERVOPACK of the same model with the same software version. Then turn the power OFF and then ON again.
A SERVOPACK fault occurred. -- The SERVOPACK may be faulty. Replace the SERVOPACK.
A.022 System Checksum Error 1 (The parameter data in the SERVOPACK is incorrect.) The power supply voltage suddenly dropped. Measure the power supply voltage. The SERVOPACK may be faulty. Replace the SERVOPACK.
The power supply went OFF while setting an utility function. Check the circumstances when the power supply went OFF. The SERVOPACK may be faulty. Replace the SERVOPACK.
A SERVOPACK fault occurred. Turn the power supply ON and OFF several times. If the alarm still occurs, the SERVOPACK may be faulty. The SERVOPACK may be faulty. Replace the SERVOPACK.
Display Name Cause Investigative Actions Corrective Actions
A.030 Main Circuit Detector Error A SERVOPACK fault occurred. -- The SERVOPACK may be faulty. Replace the SERVOPACK.
A.040 Parameter Setting Error 1
(The parameter setting was out of the setting range.)
The SERVOPACK and servomotor capacities do not match each other. Check the combination of SERVOPACK and servomotor capacities. Select the proper combination of SERVOPACK and servomotor capacities.
A SERVOPACK fault occurred. -- The SERVOPACK may be faulty. Replace the SERVOPACK.
The parameter setting is out of the setting range. Check the setting ranges of the parameters that have been changed. Set the parameter to a value within the setting range.
The electronic gear ratio is out of the setting range. Check the electronic gear ratio. The ratio must satisfy: 0.001< (Pn20E/Pn210) < 4000. Set the electronic gear ratio in the range: 0.001< (Pn20E/Pn210) < 4000.
A.041 Encoder Output Pulse Setting Error The encoder output pulse (Pn212) is out of the setting range and does not satisfy the setting conditions. Check the parameter Pn212. Set Pn212 to a correct value.
A.042 Parameter Combination Error The speed of program JOG operation (Fn004) is lower than the setting range after having changed the electronic gear ratio (Pn20E/Pn210) or the servomotor. Check that the detection conditions are satisfied. Decrease the setting of the electronic gear ratio (Pn20E/Pn210).
The speed of program JOG operation (Fn004) is lower than the setting range after having changed the setting of the program JOG movement speed (Pn533). Check that the detection conditions are satisfied. Increase the setting of the program JOG movement speed (Pn533).
The moving speed of advanced autotuning is lower than the setting range after having changed the electronic gear ratio (Pn20E/Pn210) or the servomotor. Check that the detection conditions are satisfied. Decrease the setting of the electronic gear ratio (Pn20E/Pn210).
A.044 Semi-closed/Fullyclosed Loop Control Parameter Setting Error The setting of the fully-closed module does not match with that of Pn002.3. Check the settings of Pn002.3. The setting of fully-closed module must be compatible with the setting of Pn002.3.